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News from Subaru4You
April
1st
April 1st
marks two occasions. First is the launch of the
new website (this site). There is much much more
to the new website, more interaction, more information
and more dedication. The old website was stagnant
for too long. The new website will be updated with
new information as often as possible with links to the
WRC rally site and information about the current WRC
rally. You will find parts and products on our
parts and shop pages. Over the coming weeks and
months these pages will be expanded to include new and
existing products and prices. This news page will
keep you updated with what is happening at Subaru4you
and the other news page will try to keep you abreast of
happenings in the Subaru world in general. We have
an interesting pictures page so if you have any pics.
that would be of interest to our readers then email them
in and we will see if we can publish them.
The
second announcement is that as of April 1st Subaru4you
is now a limited company. This step roughly
coincides with the appointment of a new full time
manager and the expansion of the workshop and customer
sales area (more news on that later). All in all
this is an exciting time for us and we would like to
take you long on our journey. Welcome aboard!
March 15th, 2008
Len's Black Beastie
Has a Fit
And so nearly did Len!
The story so far, see below. At the end of the day before the Donnington
track day Len and Marc bring the sponsored car into the workshop to swap out the
wheels on the Black Beast only to find that the locking wheel nuts are over
tight and will not be removed! Two hours later with the wheels swapped and
the transport truck checked over and oil topped up it was time to load up and
head home for some tea before setting off for Donnington.
On the journey up the clutch seemed difficult and there was a vibration on the
back of the truck so they pulled into the services to check but found nothing
amiss. This vibration continued off and on all the way until they were a
few hundred meters from junction 23A on the M1, (due to come off at J23A) but
the tyre burst yards before the slip road. It was now about 12.30am and woe and
behold the spare was flat too so they decided to struggle a bit further to get
off the motorway and reach the services which must have been a mile or so.
By this time the only way that the truck could restart from rest was to turn the
engine off select first gear and then restart the engine, jerking off down the
road. After making it half way up the slip road they realised that it was a job
too far, so the track car was unloaded to give the remaining tyres a chance to
make the last half a mile or so (twin wheel rear axel).
At the service under the light of the canopy with the truck jacked up they
started to remove the offending wheel but found that it was seized onto the hub
and despite beating it with a large hammer from the inside it was not going to
move. This then meant that the drum and wheel bearing had to be removed as well
and once off the centre hub had to be beaten from the wheel rim.
The spare was pumped up at the pump on the forecourt and they attempted to fit
it to the hub but attempt was the right word. The spare wheel rim had a
different hole diameter in the centre of it, this then wouldn't go over the
bearing boss on the hub and with tempers at breaking point all the tools, wheels
etc. went into the back of the cab and they drove off to the hotel, (now 01.45am).
The following morning still rolling along on 5 wheels they arrived at Donnington
(a short hop from the hotel) and after the pre track talk Marc was first to try
out "The Beast". Four or five laps later it was back in the pits with a
slight misfire. After changing the plugs Len took it out but after another
4 laps the coolant pressure cap was blowing steam. After replacing the cap
it was back onto the track but after another couple of laps the misfire was back
so it was a gentle drive back to the pits but unfortunately on the way there was
a very large cloud of oil smoke from the rear of the car and a severe lack of
any power. After recovery to the pits it was discovered that both the oil
and the coolant were now empty. End of track day.
Off to the tyre repair shop to get the truck tyre fixed whilst Marc tried
adjusting the clutch cable on the truck. With the wheel back on the truck
and the clutch working again they set off for home........
Halfway down the M1 the gears became difficult to select again even after
further adjustment so there was no option but to carry on. Within sight of
the M40 the clutch cable snapped!!! The rest of the journey was spent
wrestling with the gearbox in the start of rush your traffic on a Friday!
UPDATE: After stripping down the engine they found that the head gasket
had blown and caused pressurisation which in turn blew out the side of the
liner. A piece of the liner had disintegrated and been sucked around the
system destroying the heads and pistons. It's going to be an expensive
repair!!
March
11th
Many of
you will know that Len has been upgrading the black
beastie, a '95 WRX by building a 2.5 engine from a new
EJ25 block, forged pistons, H section steel con-rods,
race series shells and a standard crank. At the
top end, modified cylinder head combustion chambers, S4U
spec. valves and S4U spec. profiled cams. An in
tank up-rated fuel pump provides the fuel through an
adjustable fuel pressure regulator and modified parallel
fuel rail to 850 injectors. An S4U spec. turbo
with ceramic housing and custom made equal length
headers, bespoke twisted up pipe and down pipe, all
ceramic coated, all feed into a 3 inch bespoke de-cat
exhaust system. Helping to keep this cool is a
Front Mount Inter Cooler (FMIC). A twin plate
Exedy clutch delivers the torque.. Stopping this lot are 330mm front
disc brake set- up using 4 pot front caliper and
adjustable pedal box. The rear has a 330mm disc
conversion and 4 pot calipers.
He
finally saw the finishing post towards the end of Feb
and went to get it mapped only to blow the gearbox on
the rolling road!! Limping it back to the workshop
avoiding third gear it was back onto the ramps and out
with the box. Yep, third gear had stripped teeth.
After ordering a straight cut synchro gear kit and using
3.9-1 front diff and a matched rear LS diff and installing said
items it was time to book another rolling road session.
On March
the 10th he once again made the journey and this time
everything was successful. After a long wait he
finally made it onto the rolling road (roll on the day
when we have our own) and the ECU was mapped and the
engine tuned and the result
was..................500/500. Yes 500 Bhp with
500lbs torque!!! He came in to work the next day
grinning ear to ear. Pics. below
Before

After

February 18th
Welcome Rick
Rick joins the team at
Subaru4you. Rick will be the new manager ordering
parts, booking jobs, manning the phones and the 101
other jobs that need to be done which will free up Len
(he hopes) to manage the workshop. Rick is also
completely revamping the website (the one you are on now
is the new website).
February 1st 2008 New workshop
Hopefully by April/May 2008 we will have
expanded into the new workshop.
We are planning an expansion over the next few months.
We need more space in order to develop a customer
reception area, a parts department, a clean room and
eventually our own rolling road.
Proposed new workshop:

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